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The Begining...
When I pulled up to work one early December morning,
the first thing I saw parked out front was a 2005 Ford
Superduty. It is a well known fact that I am usually
late to work, but it was too early this day for a customer
to already be there. I did what any 4x4 guy would do.
I crawled underneath and checked out the brand new coil
spring suspension design. I also got a good look at
the new Dana 60 with larger hubs and factory crossover
steering. The leather interior, sunroof, and auto sliding
back window also caught my attention.
Finally, I began to get a sneaking suspicion as to
whom the truck belonged to. Phil, (who works at WFO),
had been mumbling something about getting a new truck
for the past few weeks. Due to the fact that he mumbles
about crap all day long, we didn’t really think
anything of it. I think this time he actually followed
through!
Yep, sure enough, it was Phil’s! We took it to
lunch that day. I will have to say that it is just a
little bit nicer than my GMC! At lunch, Phil mumbled
something else. We couldn’t quite hear him, but
I think he said something about 40” tires, coil-overs,
and smokies in front of the movie theater. It all sounded
great, but who in their right mind would cut apart a
brand new truck!
The next morning (as I walked in late again), Phil’s
truck was already on the rack. This kid was crazy! The
plasma cutter came out, and sparks started flying.
That day at lunch, we made a list of parts we would
need. It was a big list! I got on the phone and ordered
everything that afternoon. We were now committed!
The first order of business was the axle. The F-250
came stock with 3.73 gears. We wanted to run a 40”
radial tire, so we needed to lower the gear ratio. In
order to match the factory setup, we calculated that
we would have to run a 4.66. Due to the fact that larger
tires require a little more power to spin, we opted
for 4.88’s.
Since the axles were already torn out, they were easy
to get to. We started with the Sterling 10.5 rear.
The factory gears were taken out, and a new set of Sierra
gears was installed. For a traction device, the factory
limited slip differential was retained. After all, it
had less than 1000 miles on it!
In the front, our install didn’t go as smooth.
In the older ford front axles, once the unit bearing
is un-bolted, the whole axle assembly slides out. On
this new Dana 60 front, we couldn’t get the axles
out.
When we called the dealer, they didn’t know how
to do it either. They recommended tearing the seal apart
and replacing it. We ended up designing our own tool
to press the axles out. After a few hours of screwing
around, the axle assemblies finally came out, undamaged!
To our surprise, we were looking at a 35 spline inner
and outer axle assembly.
Not to mention a completely new unit bearing design.
This upgrade was just what ford needed.
With that small hurdle over, we could now install our
new gears. When we pulled the front cover, we discovered
that the front gears hadn’t even turned over yet.
The factory gear dye was still on them! We went ahead
and yanked them out. We quickly noticed the new spider
gears design. It was still a regular Dana 60 carrier,
but the spider gears were much larger than the old style.

A new set of Spicer OEM 4.88’s was installed.
Due to the fact that we decided to use OEM gears instead
of aftermarket thick gears, we were forced to change
the carrier as well. I had a 4.56 carrier from a 74
Chevy that was in perfect shape. We threw the new gears
on it and stuffed it in. Sure enough, everything set
up perfect! The cover was put back on, and the axle
re-assembled.
It was now time for design. Once again the three of
us pulled up a chair and started thinking. We had already
ordered 4 14” Sway Away, coil-over shocks.
It was just a matter of how we wanted to link it up.
The main focus was to have a truck that not only looked
good, but handled and drove just as good. After seeing
most of the trucks at SEMA this year, it was obvious
that most big truck builders were building for bling
only. A truck can only be so cool if it is trailered
to every show! This was going to be a daily driver.
We finally settled on a radius arm setup, front and
rear. This would allow for a nice soft ride, and help
the truck handle better. Due to the design of a radius
arm, it naturally keeps the vehicle from flexing. This
will act as a built in sway bar. We are not going to
take this on Rubicon, so we don’t need a true
4 link setup.
Our next decision was to do as little modification
to the original truck and frame as possible. We came
up with a design that used mostly existing holes in
the frame, and bolted in. We also wanted to keep the
option to be able to put the truck back to stock if
we ever wanted to. The only cutting and welding we ended
up doing was on the rear axle. We cut the leaf spring
perches off in order to weld on new link mounts. (perch
off 2)
In the front, new longer links were designed to attach
to the axle in the stock radius arm location. The axle
already had factory rubber bushings in it, ready to
accept our new links. At the upper end of the new links,
1 1/4” heim joints were used. The main link was
fabricated from 2”x.250 wall DOM tubing and 1/4”
plate steel. The plate was waterjet cut out, and broke
to fit around the tube. The upper, adjustable link,
was built from 1 7/8x .250 wall DOM. Everything was
fit and welded together. 
With the links built, the upper and lower coil mounts
were the next order of attention. The new Sway Away
coil-over shocks needed mounting points at the top and
bottom. The brackets were built in cardboard, transferred
to the computer, and cut out with the waterjet. 
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